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Page 12

LAARS Heating Systems

gallon of water from it. Turn off electrical power and
disconnect wires from operating control. Remove
operating control from diverting valve body and
replace with new control. Connect wires to control and
open isolation valves. Bleed air from the diverting
valve petcock, turn on electrical power and restart
boiler. The strap on type may be changed without
draining.

1P. Vent TCO

The vent TCO is a normally closed temperature

switch which functions to shutdown the burner if flue
gas temperatures exceed 180 - 200ºF (82-93°C). It is
mounted on the 3" (76mm) exhaust pipe inside the unit
between the top of the lower panel and the top. Switch
off electrical power when changing this safety.

1Q. Intake TCO

The intake TCO is a temperature switch with

normally closed contacts which open on a temperature
rise at 180°F (82°C). It is identical to the vent TCO
and functions to interrupt power to the gas valve if the
mixer tube temperature exceeds 180°F (82°C). It is
mounted on the mixer tube about 3" (76mm) above
burner flange. Switch off electrical power when
changing this safety also.

1R. Thermal Cut-Out (TCO)

The thermal cut-out is a probe type temperature

switch with normally closed contacts which open on a
temperature rise at 450°F (232°C). It is located on the
right side of the upper head with the probe extending
down into the exhaust passage between the boiler coil
and the economizer coil. It functions to interrupt power
to the gas valve if the flue gas temperatures exceed
450°F (232°C) for any reason. Switch off electrical
power when replacing.

1S. Delayed Ignition

Possible Causes - Time of occurrence

1.

High lockups on LP - occurs on start up.

2.

Gas valve regulation problem - occurs on start up.

3.

Defective burner (flameholder) - occurs primarily
on burner shutdown

4.

Natural gas orifice in LP unit - occurs on startup

High lock up pressures on LP fuel systems are

the most common cause of delayed ignitions on
Heatmaker boilers. The high LP supply pressure
results from improper second stage regulator selection
or a faulty regulator.

It can be detected by measuring the gas supply

pressure to the unit at the inlet pressure tap on the gas
valve. Use a water manometer or pressure gage with a
scale reading of at least 25 in. W.C. or 1 oz/in 2.
Install the pressure tap in the 1/8 NPTF plugged port

located above the gas inlet port on the gas valve. The
gas supply to the boiler must be shut off before making
this connection. The Heatmaker boiler is designed to
operate with supply pressures of 4-14 in. W.C. (8.1 oz/
in2) with the boiler not operating it is likely that this is
the cause of the delayed ignition. Lock up pressures
must be measured when the boiler is not operating and
preferably immediately after boiler shutdown.

Gas valve regulation problems can also cause

delayed ignitions. To detect gas valve regulation
problems it is necessary to have an inclined manometer
or a Magnehelic pressure gage. The normal gas valve
regulator setting is -0.2 IN. W.C. This should happen
smoothly without allowing pressure spikes positive
when the solenoid opens then the gas valve regulator is
faulty and may be the cause of the delayed ignition.

A defective burner (flameholder) can cause a

delayed ignition however not often. If the gas supply
pressure and the gas valve are functioning properly and
the air and gas orifices are correct the burner should be
inspected. To inspect, remove the mixer tube and the
burner will lift out of the top of the chamber. There
should be no perforations other than the punched holes.
Replace in the reverse order with new gaskets.

1T. High Gas Consumption

Improper burner operation caused by incorrect

air/fuel ratio (CO2 or high O2 out of the specified
range) will cause high gas consumption. It is most
noticeable on LP fired units with low CO2 or high O2,
however, units operating on LP or natural gas with
incorrect air/fuel ratios will not provide their best
efficiency. If no combustion analyzing equipment
(CO2 or O2) is available, an indication of the air/fuel
ration can be gotten by briefly sniffing the flue gases.
When running properly the Heatmaker’s flue gases
should have no smell. If they have a strong piercing
smell, the gas orifice is probably too small. Do not
attempt to do re-orificing without an O2 or CO2 kit.

1U. Noisy Operation

There are two principal sources of excessive

noise.

1.

Combustion

2.

Boiling (kettling or knocking)

Combustion noise can occur when the burner is

operating with a very rich or a very lean mixture. A
rich mixture (high CO2 or low O2 - gas orifice too
large) will cause a high pitched noise that is loudest at
the vent terminal. A lean mixture (low CO2 or high O2
- gas orifice too small) will cause a very uneven
rumbly noise and may sometimes be associated with a
nuisance lockout situation and a strong piercing odor
at the vent terminal. Both noises may be eliminated by
proper burner adjustment (see Burner Adjustment).

Summary of Contents for HWG-M2-250

Page 1: ...r installation and or operation will void the warranty WARNING If the information in this manual is not followed exactly a fire or explosion may result causing property damage personal injury or loss...

Page 2: ...h 10 1G BoilerControl 10 1H Stack Switch 11 1I Igniter 11 1J Transformer 11 1K Unit Pump 11 1L Blower 11 1M GasValve 11 1N TimeDelayRelay TDR 11 1O OperatingControl 11 1P VentTCO 12 1Q IntakeTCO 12 1R...

Page 3: ...ondensation temperature of the water vapor in the flue gases A circulator is built into the unit to provide enough head to circulate water through the H X s and to a secondary heating loop or separate...

Page 4: ...pical D Combustion Coil Outlet E Hot Water Outlet To Tank or System 160 170 F Typical 160 FTHERMOSTAT Figure 2a Water Flow through a Heatmaker 9600 HWG Before S N 394 068 CB Before S N 795 0014 THERMO...

Page 5: ...urner 8 Secondary Heat Exchanger 9 Primary Heat Exchanger 10 Return From Primary Loop 11 Gas Valve 12 Flow To Primary Loop A Secondary Heat Exchanger Inlet B Secondary Heat Exchanger Outlet C Primary...

Page 6: ...ow Through Heatmaker 9600 43 INTAKE TERMINAL 50 WALL PLATE AIR INTAKE 45 WALL PLATE 44 EXHAUST TERMINAL EXHAUST AIR ORIFICE GAS ORIFICE GAS 1 COMBUSTION COIL 2 ECONOMIZER 7 FLAMEHOLDER 46 EXHAUST ASSE...

Page 7: ...9600 CB HWG Service Manual Page 7 Figure 4 Cut Away View of Heatmaker 9600 Figure 5 Control Box...

Page 8: ...nd input desired Part Description Part 23 Jacket Front Removeable 10 402 24 Jacket Top 10 406 25 Jacket Bottom 10 010 26 Control Boiler Integrated 2400 224 27 Transformer 40 VA 2400 006 28 Time Delay...

Page 9: ...minal and at least 6 152mm into the flue pipe The unit must operate for 5 minutes before taking a sample Take a sample and determine the CO2 or O2 CO2 8 to 8 5 natural gas O2 7 to 6 CO2 9 to 9 8 propa...

Page 10: ...ostatically controlled device which keeps the primary heat exchanger H X from operating in the condensing mode When return water from the storage tank or the system is below 130 F 54 C the diverting v...

Page 11: ...d unplug the power wires from the blower motor Disconnect intake exhaust vents and remove top jacket Remove the six bolts and nuts from the blower discharge flange and the four nuts from the blower in...

Page 12: ...n the gas valve The gas supply to the boiler must be shut off before making this connection The Heatmaker boiler is designed to operate with supply pressures of 4 14 in W C 8 1 oz in2 with the boiler...

Page 13: ...se the flame signal The control then causes a restart and if the flame signal is sensed on the restart then the burner will operate again The intermittent sending and losing of the flame signal by the...

Page 14: ...solution is no longer foamy 7 Shut off pump and disconnect from hose Carefully drain solution from hoses and connect city water to lower hose to flush combustion coil Flush for approximately 5 minutes...

Page 15: ...on and no indicator lights are flashing check for an open vent TCO operating control or safety limit switch For additionaltroubleshootinginformationrefertothe trouble shooting flow charts on the page...

Page 16: ...VOLTAGE 120 VAC BETWEEN BLACK AND WHITE WIRES AT BACK OF 120 VAC CONNECTORON BOILERCONTROL DIDBOILERRUNTHROUGHA COMPLETE CYCLE AS DE SCRIBED IN SEQUENCE OF EVENTS PAGE 20 TESTLIMIT CIRCUIT PAGE 17 PUM...

Page 17: ...OHMSCALE CONTINUITY CONTINUITY CONTINUITY NOCONTINUITY OHMS NOCONTINUITY TESTING LIMIT CIRCUIT YOU MUST COMPLETE PAGE 16 FIRST NOTE AFTER COMPLETEING LIMIT CIRCUIT TESTING PLUG IN CONTROL PLUG AND REC...

Page 18: ...EAVESETC AGAINST VENTTERMINAL CYCLE BOILER MANY TIMES TO TRY TO CREATE A MALFUNCTION CLEAR BLOCKAGE AND RECYCLEBOILER CHECKSTACKSWITCH BLOCKAGE EXISTS NO BLOCKAGE NO YES YES NO RED PURGE LIGHT FLASHIN...

Page 19: ...TSTACKSWITCH TUBES AND CHECK FOR CONTINUITYBETWEENSTACK SWITCHTERMINALSWITH BLOWEROPERATING CHECKFORVENTOBSTRUCTIONS CLEAROBSTRUCTIONS RECONNECTTUBES ELEC TRICALWIRESTOSTACK SWITCH START BOILER RUN TH...

Page 20: ...SSURETAP ON GAS VALVE PRESSURE DURING BLOWER OPERATIONWITHOUTGASFLOW VALVE FLAME LIGHT NOT LIT IS 4 IN W C CHECK FOR VOLTAGE 120 VAC ATBLOWERWIRECONNECTOR WITHIN5MINS AFTERGREEN LIGHT BLOWER O K REPLA...

Page 21: ...G LITE CHECKCOMBUSTION CHECKIGNITER IGNITEROK CHECK FOR GAS FLOW IS METER MOVING REPLACE IGNITER REPLACEINTEGRATEDBOILERCONTROLP N2400 224 INSTALL CORRECT ORIFICES BOILERCYCLESTHROUGHTHREECYCLESAFTER...

Page 22: ...L PLUG CN6 THERE IS 120 VAC AT CIRCULATOR PLUG CN5 TURNUPT STATORAQUASTATOR CORRECTSTATPROBLEM NO YES NO YES SEETROUBLESHOOTING CHART PAGE 16 THERE IS 120 VAC AT PUMP REPLACEBOILER CONTROLP N2400 224...

Page 23: ...23 Figure 9 9600 Ladder Diagram Figure 10 9600 Wiring Diagram Caution Label all wires prior to disconnection when servicing controls Wiring errors can cause improper and dangerous operation Verify pr...

Page 24: ...sure of 9 3 Remove blower and inspect flameholder burner for hole 4 Check that the blower flanges and gas piping are sealed D OCCASIONAL LOCKOUTS Requires interruption of power to re start or reset of...

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