Chapter 6 Troubleshooting
125
Ch
ap
ter 6
No. Fault ID
Failure type
Possible causes
Solutions
parameter is timeout
20 Err.20
Disk code
fault
1.the encoder is damaged
2.PG card is abnormal
3.the encoder model does not
match
4.the encoder connection has
error
1.replace the encoder
2.replace the PG card
3.correctly set the encoder model
according to the Actual
conditions
4.eliminate the line fault
21 Err.21
EEPROM
read and
write fault
EEPROM chip is damaged
Replace the main control panel
22 Err.22
Inverter
hardware
fault
1.overvoltage
2.overcurrent
1.eliminate overvoltage fault
2.eliminate overcurrent fault
23 Err.23
Short-circuit
to ground
fault
Motor short to ground
Replace the cable or motor
26 Err.26
Cumulative
running time
arrival fault
Cumulative running time
arrival fault
Clear history information by
using initialization function
parameters
27 Err.27
Custom fault
1
Input custom fault 1 signal
through the multi-function
terminal DI
Reset run
28 Err.28
Custom fault
2
Input custom fault 2 signal
through the multi-function
terminal DI
Reset run
29 Err.29
Total power-
on time
arrival fault
Total power-on time reaches
the set value
Clear history information by
using initialization function
parameters
30 Err.30
Load drop
fault
The inverter running current is
less than F8.31
Confirm whether the load is
removed or not or the settings for
parameter(F8.31, F8.32) accord
with the Actual operating
conditions
31 Err.31
PID feedback
loss when
running fault
PID feedback is less than the
set value of E2.11
Check PID feedback signal or set
E2.11 to an appropriate value
40 Err.40
Quick
current
limiting fault
1.whether the load is too large
or the motor stall occurs
2.the type selection of inverter
is small
1.reduce the load and check the
motor and its mechanical
conditions
2.choose the inverter with large
power level
41 Err.41
Switch motor
when
running fault
Change current motor through
the terminal when the inverter
is running
Switch motor after the inverter
stops
42 Err.42
Too large
speed
deviation
fault
1.the setting for Too Large
Speed Deviation
parameters(F8.15, F8.16) is
unreasonable.
2.the setting for encoder
parameters is incorrect
3.the parameter was not
1.reasonably set the detection
parameters
2.correctly set encoder
parameters
3.perform identification for the
motor parameters