SINAMICS DCM
List Manual (LH8), 02/2015, 6RX1800-0ED76
983
4 Faults and alarms
4.2 List of faults and alarms
1 hex:
The Control Unit was withdrawn from the Power Module during operation, although the encoderless safe motion
monitoring functions are enabled. This is not supported. After re-inserting the Control Unit in operation,
communications to the Power Module no longer possible.
20A hex:
The Control Unit was inserted on a Power Module, which has another code number.
20B hex:
The Control Unit was inserted on a Power Module, which although it has the same code number, has a different
serial number.
601 hex:
The Control Unit was inserted on a Power Module, whose power/performance class (chassis unit) is not supported.
Remedy:
Reinsert the Control Unit (CU) or the Control Unit adapter (CUAxx) onto the original Power Module and continue
operation. If required, carry out a POWER ON for the CU and/or the CUA.
Reaction upon A:
NONE
Acknowl. upon A:
NONE
F30080
Power unit: Current increasing too quickly
Message value:
Fault cause: %1 bin
Message class:
Power electronics faulted (5)
Drive object:
CU_DC, CU_DC_R, CU_DC_R_S, CU_DC_S, TM150, TM15DI_DO, TM31
Reaction:
NONE
Acknowledge:
IMMEDIATELY
Cause:
The power unit has detected an excessive rate of rise in the overvoltage range.
- closed-loop control is incorrectly parameterized.
- motor has a short-circuit or fault to ground (frame).
- U/f operation: Up ramp set too low.
- U/f operation: rated current of motor much greater than that of power unit.
- infeed: High discharge and post-charging currents for voltage dip.
- infeed: High post-charging currents for overload when motoring and DC link voltage dip.
- infeed: Short-circuit currents at power-up due to the missing line reactor.
- power cables are not correctly connected.
- power cables exceed the maximum permissible length.
- power unit defective.
Additional causes for a parallel switching device (r0108.15 = 1):
- a power unit has tripped (powered down) due to a ground fault.
- the closed-loop circulating current control is either too slow or has been set too fast.
Fault value (r0949, interpret bitwise binary):
Bit 0: Phase U.
Bit 1: Phase V.
Bit 2: Phase W.
Remedy:
- check the motor data - if required, carry out commissioning.
- check the motor circuit configuration (star-delta)
- U/f operation: Increase up ramp.
- U/f operation: Check assignment of rated currents of motor and power unit.
- infeed: Check the line supply quality.
- infeed: Reduce the motor load.
- infeed: Correct connection of the line reactor.
- check the power cable connections.
- check the power cables for short-circuit or ground fault.
- check the length of the power cables.
- replace power unit.
For a parallel switching device (r0108.15 = 1) the following additionally applies:
- check the ground fault monitoring thresholds (p0287).
- check the setting of the closed-loop circulating current control (p7036, p7037).
Summary of Contents for SINAMICS DCM
Page 1: ...s SINAMICS SINAMICS DCM List Manual 02 2015 Edition Answers for industry ...
Page 2: ......
Page 1192: ...A Appendix A 2 List of abbreviations SINAMICS DCM 1192 List Manual LH8 02 2015 6RX1800 0ED76 ...
Page 1202: ...Index SINAMICS DCM 1202 List Manual LH8 02 2015 6RX1800 0ED76 ...
Page 1203: ......